Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource...

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Kenosha Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: Curt Czarnecki, P.E. Kenosha Water Utility Presented By: Joseph Hughes, P.E. Centrisys Corporation MIWEA June 21 st , 2016

Transcript of Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource...

Page 1: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Kenosha Wastewater Treatment Plant -Energy Optimized Resource Recovery

Project

Prepared By:

Curt Czarnecki, P.E. Kenosha Water Utility

Presented By: Joseph Hughes, P.E.

Centrisys Corporation

MIWEA June 21st, 2016

Page 2: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

• The entire Kenosha Water Utility (KWU) Staff, including:

• Ed St. Peter, Curt Czarnecki, Melissa Arnot, Katie Karow, &

Tom Tetzlaff

• J. F. Ahern – General Contractor

• Pieper Power – Electrical Contractor

• CD Smith – Civil Contractor

• Donohue & Associates – Engineer including Dennis Dineen &

Allen Williams

• Centrisys Corp. including Geoff Harvey & Christine Smith

• CNP – Gerhard Forstner

Thanks & Acknowledgement

Page 3: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

• Kenosha Water Utility (KWU) and Wastewater Treatment Plant

(WWTP) Overview

• Drivers for Energy Optimized Resource Recovery Project

• Technology Overview

• Preliminary Results

• Economics (Added Value)

• Conclusion

Presentation Outline

Page 4: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

WWTP Service Area Overview

• Population: 110,000

• Service Area: 85.7 mi2 (222 km2)

• Collection System – Gravity Sewer System: 332 mi (535 km)

– Lift Stations: 13

• Permitted Annual Average Daily Flow: 28.6 MGD (1.253 m3/s)

• 2015 Annual Average Daily Flow: 21.9 MGD (0.961 m3/s)

• Effluent Discharge: Lake Michigan

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Page 6: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

WWTP Loadings Average Day (Current Loadings Based on 2015 Data): • BOD

– Influent: 32,910 lbs/day (180 mg/l) – Effluent: 2,475 lbs/day (13 mg/l) – 92% Removal

• TSS – Influent: 32,863 lbs/day (180 mg/l) – Effluent: 1,415 lbs/day (8 mg/l) – 96% Removal

• Ammonia – Influent: 4,881 lbs/day (27 mg/l) – Effluent: 530 lbs/day (3 mg/l) – 89% Removal

• Phosphorus – Influent: 533 lbs/day (3 mg/l) – Effluent: 85 lbs/day (0.5 mg/l) – 84% Removal

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Sludge Characteristics Primary Sludge:

– Average Flow: 68,620 gal/day (260 m3/day) – Solids Concentration: 3.3% – Solids Production: 19,020 lbs/day (8,626 kg/day) – Volatility: 77%

Waste Activated Sludge (WAS): – Average Flow: 151,350 gal/day (570 m3/day) – Solids Concentration: 1.05% – Solids Production: 13,010 lbs/day (5,900 kg/day) – Volatility: 72%

Digested Sludge – Solids Concentration: 2.7% – Volatile Solids: 54% – Volatile Solids Reduction: 60% – Sludge to Landfill (2015): 2,500 dry US tons, 2,270 dry metric tons

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Motivation Behind Project

• Aging WWTP infrastructure

• An effort to combat ever rising utility costs:

– Natural Gas

– Electricity

• Reduce or eliminate landfill disposal fees

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Project Objectives

• Increase biogas production

• Generate electricity from biogas

• Achieve 90% dry and Class A biosolids

• Utilize waste heat as the main thermal energy supply

• Maintain existing effluent quality

• Maintain or decrease noise, odor and particulate levels

Page 10: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Design Approach • Wisconsin allows for design/build approach on

resource recovery projects • Design/Build was utilized due to the varying

technologies and complexity of the project. • In the RFP the design/builder was tasked with the

following: – Preparation of the design – Assisting KWU in obtaining all necessary permits – Procuring, constructing and installing all components – Integrating the new system with the existing plant

SCADA network – Startup and commissioning – Preparation of O & M manuals – Warrantying the system

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Page 12: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Anaerobic Digestion Modifications

Before Project After Project

Digesters 4 primary

2 secondary

2 primary

1 secondary

Total Capacity 633,550 ft3 319,650 ft3

Mixing Condition Unmixed Fully mixed with mechanical

hydraulic mixing

Sludge Feed

Operation

Batch feeding operation based

on 8-hour shifts Continuous feed

Feed Primary (3.3% TS)

WAS (5.0% TS)

Primary (7% TS)

WAS (7% TS)

HRT in digesters Primary=30 days

Current operation:

Primary=17 days

Ultimate Operation:

Primary=22 days

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Mechanical Hydraulic Mixing Rotamix by Vaughan Company

System consists of: • Chopper pump • Internal piping • Six nozzles (per digester) Benefits: • More even heating of

contents • Improved volatile solids

reduction • Increased gas production

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Primary Sludge Thickening Centrifuge THK 200 by Centrisys Corporation

Before Project: Gravity thickened sludge (3.3% TS) pumped directly from the clarifiers into the digesters Operational Characteristics • Sludge Feed: 3.1% TS • Cake Material: 6.1% TS • Avg. Power Consumption:

5.7 kW • Capture Rate

• Without Polymer: 89% • With Polymer: 98%*

*Emulsion Cationic Polymer 46% active

@ 0.5 gallons/hour

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WAS Thickening Centrifuge THK 200 by Centrisys Corporation

• Prior to our partnership: A DAFT system was utilized to thicken the WAS flow stream from 1% TS to 3.5-4.0% solids before being pumped into the digesters

• A WAS thickening centrifuge was previously pilot tested and installed in 2011 – Due to downstream

limitations the WAS flow stream was thickened to roughly 5% solids with the thickening centrifuge

– This project allowed us to further thicken the WAS flow stream to 7% solids

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WAS Thickening Centrifuge Installation

Operational Characteristics • Sludge Feed: 1.1 - 1.3%

TS • Cake Material: 6.9% TS • Average Power

Consumption: 13.6 kW • Capture Rate: • Without Polymer: 90% • With Polymer: 97%*

*Emulsion Cationic Polymer 46% active @ 0.2 gallons/hour

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Thermo-Chemical Hydrolysis PONDUS by CNP-Technology Water and Biosolids Corporation

Components of Hydrolysis Process:

• Thermo: TWAS is heated to 140 - 160oF (60 - 70oC)

• Chemical: 1.5 to 2.0 liters of caustic soda (50% concentration) is injected per 1 m3 of TWAS

• Detention Time: Circulation through the reactor and heat exchanger for 2 to 2.5 hours.

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Thermo-Chemical Hydrolysis

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Thermo-Chemical Hydrolysis

pH

• Upon addition of caustic soda pH = 11 (+/-)

• Following hydrolysis process pH = 6.8 to 7.0

• Hydrolysis process breaks down the cell walls and releases internal organic acids which brings the pH of the flow stream back to neutral.

• Hydrolysis causes the pH adjustment and therefore no additional chemical addition is necessary prior to anaerobic digestion process.

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Thermo-Chemical Hydrolysis

Thermal Efficiency • The blending of hydrolyzed TWAS and unheated

thickened primary sludge results in a final temperature of roughly 40oC (100oF) which is ideal for the mesophilic anaerobic digestion process

• All thermal energy required for the hydrolysis process is transferred into the digesters.

Atmospheric Pressure • The entire hydrolysis process is completed at

atmospheric pressure Additional Volatile Solids Reduction • Volatile solids reduction of 60% (before) and 65%

(currently) Increased Dewaterability of Digested Sludge

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PONDUS Reactor Installation

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PONDUS Heat Exchanger

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Thermo-Chemical Hydrolysis

• Reduced Viscosity Provides for: – Lower mixing energy requirements

– Higher digester loading rates

1

10

100

1000

10000

0 4 8 12 16 20

Dra

ina

ge

tim

e (

se

c)

Nozzle diameter in mm

Sludge viscosity tests at KWU (compensated for sludge density)

water 1 mPa s 20,0 °C 1000,0kg/m³

glycerol 99,5 %tig, 1480 mPas 19,6 °C, 1260,0 kg/m³

WAS Kenosha 19,6 °C, TS6,5% , GV 70,0% , 1026,3kg/m³

drain flow hydrolysisc138/input 15 gpm 71,0 °C,TS 6,5% , GV 70,0% ,1005,3 kg/m³

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Biogas Production

149,012

155,826 152,956 155,384

192,502

181,039 185,771

176,316 184,358

178,676

0%

4% 3% 4%

23%

18% 20% 15%

19% 17%

0%

10%

20%

30%

40%

50%

100,000

120,000

140,000

160,000

180,000

200,000

220,000

240,000

2012 2013 2014 2/22/16 -3/6/16

3/7/16 -3/20/16

3/21/16 -4/3/16

4/4/16 -4/17/16

4/18/16 -5/1/16

5/2/16 -5/15/16

5/16/15 -5/29/16

Cu

bic

fe

et

pe

r d

ay

Additional Biogas Production

2-Week Average Daily Biogas Production

Increased Biogas Production from 2012 level (Contract Base Year)

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Biogas Conditioning Gas conditioning and siloxane removal by Unison Solutions

• Before Project: Raw biogas was utilized by – Raw water pump engines

– Hot water boilers

– Flared to the atmosphere

• A package system was incorporated to condition and compress the biogas – moisture

– particulates

– siloxane

Page 26: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Electric & Thermal Energy Generation

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Electric & Thermal Energy Generation CHP Generators by Kraft Power

• Before Project: – All electricity was purchased exclusively from the local utility. – All heat was provided by our boilers using either natural gas or biogas

as their fuel source.

• Two combined heat and power (CHP) generators were installed to utilize the biogas as a fuel source to generate electrical as well as thermal energy.

• The CHP units are each capable of producing: – 330 kW of electrical energy – 422 kW of thermal energy

• The electricity produced will power the new system as well as supply the excess electricity to the main plant power network for beneficial use elsewhere throughout the plant.

• The thermal energy will be utilized by the PONDUS system, the compact belt dryer and the central WWTP heating loop.

Page 28: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Isometric Project Overview Heat Biogas Electricity Biosolids

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Biosolids Dewatering CS 21-4HC Centrifuge by Centrisys Corporation

• The centrifuge was installed in 2009 & replaced three plate and frame presses.

• This project met or exceeded all design criteria and provided a payback of one year!

• The dewatering centrifuge has historically been fed digested sludge with a 2.7% TS concentration and consistently achieved 26-29% TS on the cake material.

Page 30: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Centrifuge Room

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Drying of Biosolids Compact belt dryer by Sulzle-Klein

• Previously dewatered biosolids went to local landfill

• Now, biosolids are dried using the recovered heat from the co-generation units as the thermal supply.

• The belt dryer achieves all the requirements of Class-A and KWU is currently in the process of getting our final biosolids product re-classified with the Wisconsin Department of Natural Resources.

• The dried product is discharged into a conveyor system and automatically deposited into the bed of a dump truck.

Page 32: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Drying of Biosolids

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Drying of Biosolids

Distributor extrudes the biosolids into noodle-like strands to maximize the surface area for maximum evaporation capacity

Page 34: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Drying of Biosolids

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Odor Control KWT 1000/1300 by Sulzle-Klein

• Treats the exhaust air from the belt dryer, the buffer & mix tanks, the PONDUS reactor, and the thickening & dewatering centrifuges.

• Water cools the exhaust air and removes particulates.

• Sulfuric acid neutralizes ammonia odors.

• Caustic soda neutralizes sulfur compounds such as mercaptans.

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Other Items Incorporated Into Project

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Other Items Incorporated Into Project

Page 38: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Other Items Incorporated Into Project

Page 39: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Other Items Incorporated Into Project

Page 40: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Other Items Incorporated Into Project

Page 41: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Other Items Incorporated Into Project

Page 42: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Other Items Incorporated Into Project

Page 43: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Estimated Added Value Criteria Daily Annual Unit Cost Unit Annual Savings

On-Peak Electricity

(kWh) 4,752 1,734,480 $0.07660 per kWh $132,861

Off-Peak Electricity

(kWh) 8,448 3,083,520 $0.05238 per kWh $161,515

Electric Demand (kW) 550 6,600 $12.65 per kW $83,490

Electrical Total $377,866

Cake Sludge

(wet tons) 25 9,249 $38.01 per ton $351,554

Disposal Total $351,554

TOTAL Value $729,420

Page 44: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Grant from Local Utility

• Due to the nature of the project KWU was awarded over $500,000 in grants for implementing the new biosolids process from Focus on Energy.

• The installation of the thermo-chemical hydrolysis system, co-generation units, and LED lighting all qualified for the largest grant this organization awards to an individual project.

Page 45: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Conclusion

Through innovative thinking KWU was able to:

–Become more energy efficient

–Less reliant on purchased electrical and thermal energy, reducing operating costs

–Produce a higher quality end product (Class A Biosolids)

Page 46: Kenosha Wastewater Treatment Plant Energy … Wastewater Treatment Plant - Energy Optimized Resource Recovery Project Prepared By: ... Director of Engineering Services

Questions? Curtis Czarnecki, P.E.

Director of Engineering Services

Kenosha Water Utility

4401 Green Bay Road

Kenosha, WI 53144

Phone (262)653-4306

[email protected]

Joe Hughes Project Manager Centrisys Corp.

Phone: (262) 716-9949 [email protected]